![]() ![]() It said the lack of damage to the plug where the bolts were supposed to attach it to the fuselage of the plane pointed to the conclusion that the bolts were missing at the time of the flight. In their 19-page preliminary report released Tuesday, NTSB investigators included observations from a laboratory disassembly of Alaska 1282’s door plug, which fell 16,000 feet into an Oregon backyard. That includes more inspections, giving the 737 teams more time “to focus on and implement quality improvements,” and bringing in outside safety experts to assess its operations. We simply must do better for our customers and their passengers.”īoeing said it was taking new actions to improve the way it makes the 737 Max 9 planes. “An event like this must not happen on an airplane that leaves our factory. “Whatever final conclusions are reached, Boeing is accountable for what happened,” said Boeing CEO Dave Calhoun in a statement. The new finding from federal investigators comes one month and a day after the January 5 incident that triggered a 19-day emergency grounding of all Max 9s, and re-ignited scrutiny of Boeing following the fatal Max 8 crashes of 20.īoeing acknowledged its responsibility for the blowout in a statement issued after the NTSB report and said it is working to make sure incidents like this do not reoccur. Investigators from the National Transportation Safety Board on Tuesday said evidence shows four bolts that hold the door plug in place on the Boeing 737 Max 9 were missing at the time of last month’s blowout on Alaska Airlines flight 1282. ![]()
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